This falls in the "WOW...just WOW" category.
Enjoy:
"...This is what I heared so far (info from several sources put together by me): At NAS Whidbey Island, Washington, P-3C 161331 was doing a Functional Check Flight. They shut down #1 engine. With #1 off, #2 engine exhibited vibrations and was shutdown. With two engines off on the same side the aircraft stalled. 7 G's were reported to pull it out of the stall. 45 consecutive rivets were pulled out on the stbd wing during the 7 G pull out (rolling pull), after peaking at negative 2.4g's as well. They did five spin rotations from 5500 ft- - they bottomed out "between 50 and 200 ft"!! They could see the inside of the fuel tanks when they landed. They were at 160 KIAS, appr flaps during a prop fails to feather drill on #1 when #2 started surging. They bagged #2, but while doing so got to 122 KIAS. When they added power, they were way below VMC air, and departed. SDRS recorded the flaps being raised and the landing gear being cycled down and then back up. Aircraft released all the fuel in tank #3 when it appears that the seam between planks 3 and 4 split. Tank #4 also lost its fuel load when plank #1 separated from rest of the aircraft wing. Regards, P-3 Orion Research Group - The Netherlands..
More pics
http://www.network54.com/Forum/21914...nfo+and+Photos http://navlog.org/p-3_strike.html